Paperweight Rebuild REV03

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bggrnchvy

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I got the axle back in the truck even if I wanted to be in the pool staying cool instead.

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Had to pop the passenger upper link out of the truck and bust the jam nuts loose to collapse it to fit.

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Lots of clearance at full bump. Should more than account for frame deflection when it hits the stops (factory 1/2t frame rails are noodles, I swear).

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Took the oil cooler diverter block out and cut the hardlines off (there were kinked). Milled the bosses down to get the remaining tube fittings out, except one of them decided to prematurely leave its home, hence the damage to the face in pic 1. It jammed up the end mill to the block and kicked it sideways in the vise. No matter, faced it to get the depth to the threads down. Drilled the ports to .563 and tapped it to 3/8NPT for the 3/8NPT to -8 adapters.

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The t-case adapter and clocking ring got a lot of scotchbrite time. Going to use gaskets this time and hope for perfect sealing and less mess the next time I pull the combination.

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Lastly the adapter fittings for the tranny cooler hsowed up so I pulled the factory ones and put them in.
 

bggrnchvy

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Last night it was time to fix the transmission pan bolts. The previous owner drilled all the threads out and put in 5/16-18 helicoils...or tried at least. He both forgot/neglected to knock out the tang and used bolts just long enough to hit the tang. The combination reulted in several back out a couple threads, one stripping completely and one galled bolt that sheared the head :(

The two types of offenders:

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Broken bolt.

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Threadless oversized hole/bad helicoil.

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Broken stud was an easy fix. Cover in a couple layers of aluminum foil, bust out the welder and a 1/2" nut and blaze it on. Turned right out and the helicoil itself is fine.

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The other holes needed these, externally threaded key locking inserts, commonly called by a tradename: Timsert.

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Pretty basic really, drill and tap the hole to a standard thread proscribed by the size of the internal thread and wall thickness of the insert selected. Countersink the lip to allow it to go below flush and thread the insert in.

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Then using the tool supplied, drive the locking tabs into the base material locking the external threads in place. Done!

Planning to switch back to a stock sheetmetal pan as well.
 

bggrnchvy

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Don't mind me, just cutting up more parts...

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Did I need that? Well at least I have campfire goodies now.

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Phew, I didn't need it.

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Ready for some finish filing after rough contouring and for me to plot my exit (or inlet) hole for the suction supply hardline to the pump.
 

bggrnchvy

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Step forward, step backwards, sigh.

In our last installment we left our intrepid hero needing a stock transmission pan to replace his deep sump cast aluminum unit as a result of draining the pickup during steep climbs.

Apparently the only current production 80e pans don't fit pre 97 80e's.

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New 97+ pan, notice the ramp at the back?

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See the diagonal tube headed back across the picture?

In the post 96 transmissions GM moved the return cooler port to the back of the 80e instead of pairing the output and inlet at the front. The goal was to keep the rear planetaries better lubricated. Previously they used an internal lube tube (the diagonal in two pictures above) to accomplish a similiar function. With the internal tube gone they redesigned the pan and ramped the back to absorb the volume the tube took up. Hence late pans don't fit early transmissions.

I managed to locate an early pan in a city close by on ebay. Had that gentleman drop it in the mail for delivery today. With the pan on I'll install the transmission and BU54 converter.

In other news, I finally welded in the plug for the old feed hole on the power steering pump and threaded in the plug on the other feed hole.

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The idea is that I may in the future need to add even more incoming volume to keep the pump balance happy, so threadedin a pipe plug allows me to modify tht in the future.

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Lastly I put the pump back together using a crosssection diagram to get orientation right as I took it apart to long ago to remember everything 100%.

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Working on reservoir supply tube routing in the next few days.
 

DRAGGIN95

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Looking good man, that suck's about the pan, but at least you got it worked out, and we all know now that the 97+ pan doesn't fit the older 80E.
 

bggrnchvy

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Haven't done a lot recently, but hoping to pick up quickly here.

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Accesory bracket and accesory bolted in. Crossover tube doesn't clear the alternator, going ot have to owkr that out.

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Routing the PS pump feed line was a pita as it's -12 and inbetween the belt and fan (yes the mech fan is staying for the time being). Luckily a hard 90* off the pump followed by a 90* swept fits around everything. Hopefully the hard 90* flows well enough.

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Tranny is in for the time being. It's a pain lifting that thing and then getting it in without an extra pair of hands to work the jack but it's in there. I found I was missing on eof the alignment dowels so now that I have that in hand I have to back the tranny off and hope freezing the sucker gets in in with a light tap.

Working on the PS cooler mount this evening and probably tomorrow so I can put all these darned expensive fittings to use.
 

bggrnchvy

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dedication.com my man

Indeed, it's becoming a test of will.

Busy weekend of progress.

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Started by pulling the tranny off to put in the replacement dowel pin, shortly followed by tossing the t-case in behind it after cleaning the wee out of the FHCS that mount the clocking ring as well as the t-case mating surface and blind tapped holes so the Locktite would bite. Two gaskets and consistent torque and it may seal this time.

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Bent some leftover tube and welded some thin plates to make a mounting frame for the cooler.

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The belly crossmember had previously just been tapped to 1/2-20 through the 1/8" wall. Enough strikes on the cap screws holding the skid plate on meant a lot of stripped holes.

To fix it I needed to devise an easy way to weld some nuts in. The simplest solution I had was to grind the points on the nuts down a touch to make them 12 points basically. Then I opened the threaded holes up to 3/4" and took a chamfering tool and chamfered until the 3/4" lip was .005-.015'ish thick. I threaded the modified nuts onto a fully threaded bolt and used a hammer on the bolt to drive the nuts in. The 12 external points just broached through the chamfered edge resulting in a press fit that held them in place and I had good void to fill with weld so I didn't feel bad grinding them flat.

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All done, repeat 6x.

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Then I went to put the frame in...lets just say I called it a night on Saturday. Seems the adapter plates moved the drivetrain forward 1-1/2"s.

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Kevin came out Sunday, mostly so his wife could go hang out in the pool with my significant other, but partially to give me a hand. He knocked out a cooler mount, modded the ECM mount for the early LS computer, got the relay block mocked up waiting on hardware and mocked up the factory'ish intake and helped me decide to just relocate the battery tray. Thanks buddy.

While he was doing that I was trying to fix the issues that the motor mount plates created. The t-case was hitting the back of the front 2x3 piece of tube and the ghetto mounting foot for the tranny adapter wasn't long enough.

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I notched and plated in the relief for the t-case a well as removed the entirety of the ghetto mount.

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I cut a piece of 1/8" laying around for a cover plate and integral shim, then made a C out of some 2x2 .120 and burned it all together and made my top side holes with counter bores on the back side for clearance.

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Finished it off later last night after everybody had left by blazing it on. Now lets just hope my tape measure operating skills are up to par, eek.
 

bggrnchvy

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Busy weekend. Some stuff got done on the truck, but I was hoping to key up the motor and fire it off and that didn't happen, maybe this week.

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Belly pan is in.

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Cut down the inspection cover to make it fit behind the LS truck oil pan.

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Got it bolted in after a littler persuasion. Removing the rib let a lot of internal casting stress through and it splayed the cover open.

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I ran the tranny cooler lines as well. A couple of cable ties to keep them together and that's buttoned up.

Currently chasing wires, joy.

Oh and for your amusement, our friends debacle:

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600 5.9L with tuner and grossing 24k matted results in broken rings, scored cylinders and a whole lot of oil burnoff.
 
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