So, got several things done this weekend. First on the list was the torque converter. My little brother and I dropped the trans out and pulled the converter. Input shaft looked good, no issues or damage to speak of. Flexplate was fine with no warpage or cracking visible, so it stayed. Rear main seal was dry as Melba Toast, so I left that alone as well. Looks like my oil leaks are likely the oil cooler adapter and the pan, which I will address.... some day. Will likely pull the engine out and reseal one day, maybe roll in new bearings for ***** and giggles. Filled the converter with some synthetic ATF that I get from work, and installed. I realized after I pulled the old converter that I had, in my haste, completely forgotten to get a new input shaft o-ring. This resulted in a heart felt cussing fit that put me in a damned foul mood. Coffee and cigarettes were consumed. More cussing. Eventually I got over it and, with time pressing, popped the new converter on the trans. After bolting her back up and dealing with the cooler line clips (copious cussing) and myriad brackets and clips that go on the studs of the bellhousing bolts (sailors were blushing, somewhere) I set her down and filled the trans. Ran through the gears, topped off the fluid. Ran gears again, topped off fluid. Rinse and repeat. Finally got the hot fluid level in spec and.... and... still some lockup slippage under moderate throttle. Somewhere, beyond this world perhaps, the guy that designed the 4L60/700R4 sat up with a start as his ears burst into flames. I was hot. I was DAMNED hot. My fault for failing to order everything I needed, absolutely. But... it felt good at the moment. Once my blood pressure came back to cruising altitude, I dragged my ass back home and had a beer to salve my wounds. If I have to pull the damned trans out to replace one cheesy ass o-ring, so be it. Life will go on.
There was a positive note this weekend. After installing the converter I decided to finish off the AC install/service and clean the evap core. Using a calibrated thermometer I had been getting outlet temps of around 42F with an upper 60's to 70F ambient. Decent, but not good enough. Compressor was hitting low pressure cutoff and I had the feeling that my evaporator efficiency wasn't what it should be. This was confirmed by infrared thermo readings at the inlet and outlet of the evap. In an ideal system, you should have the same temperature reading at the inlet and outlet of the evaporator. Heat transfer is performed by the low pressure liquid refrigerant expanding into a low pressure gas in the evaporator with no change in temperature of the refrigerant. In practice, due to operating conditions and their effect on orifice/heat exchanger efficiencies, this isn't the case. You will usually see some rise in temps from one side to the other. If you see a DROP from the inlet to the outlet, then you generally have a flow restriction in the evap core OR poor evaporator efficiency. Poor heat exchange can result in liquid refrigerant coming out of the evaporator into the drier, which is why you can see lower temps on the outlet and have poor cooling performance.
Given all of that, I expecting some crud, but not what I found. I popped the glove box off and removed the blower motor. Reached my hand in and pulled this out:
Oi. That's a lot of crap for such a tiny heat exchanger. I decided to get a better look at things and poked by cell camera in the hole and found this mess:
ERMAGHERD! Luckily I came prepared for this eventuality:
Sprayed the evap down with this stuff and then hosed it out. And again. And again. Till we got this:
Got rid of a lot of dirt, but still had some caked on crap at the top and left. What kind of caked on crap? Hair. Dog hair, to be specific. And I've only hauled a dog once or twice in my time with das 'Burb. So some OLD dog hair. Whooped out an old tooth brush and scrubbed that **** off. And then sprayed and hosed again. And again... and again. Finally, after getting sliced up nicely by the evap fins, I reached this point:
And with that, I said, It IS Done. I put the blower back in and reassembled the rest. Results were better airflow, less fan noise, and better smelling air. Also managed to hit around 38F with the same ambient as before. So better evap efficiency too. I'll get some better weather for testing in the near future, but I think the AC is about as good as it will get. Will be installing the condenser fan to see if I can keep the idle AC temps down.
And that's the way it was...
There was a positive note this weekend. After installing the converter I decided to finish off the AC install/service and clean the evap core. Using a calibrated thermometer I had been getting outlet temps of around 42F with an upper 60's to 70F ambient. Decent, but not good enough. Compressor was hitting low pressure cutoff and I had the feeling that my evaporator efficiency wasn't what it should be. This was confirmed by infrared thermo readings at the inlet and outlet of the evap. In an ideal system, you should have the same temperature reading at the inlet and outlet of the evaporator. Heat transfer is performed by the low pressure liquid refrigerant expanding into a low pressure gas in the evaporator with no change in temperature of the refrigerant. In practice, due to operating conditions and their effect on orifice/heat exchanger efficiencies, this isn't the case. You will usually see some rise in temps from one side to the other. If you see a DROP from the inlet to the outlet, then you generally have a flow restriction in the evap core OR poor evaporator efficiency. Poor heat exchange can result in liquid refrigerant coming out of the evaporator into the drier, which is why you can see lower temps on the outlet and have poor cooling performance.
Given all of that, I expecting some crud, but not what I found. I popped the glove box off and removed the blower motor. Reached my hand in and pulled this out:
You must be registered for see images attach
Oi. That's a lot of crap for such a tiny heat exchanger. I decided to get a better look at things and poked by cell camera in the hole and found this mess:
You must be registered for see images attach
ERMAGHERD! Luckily I came prepared for this eventuality:
You must be registered for see images attach
Sprayed the evap down with this stuff and then hosed it out. And again. And again. Till we got this:
You must be registered for see images attach
Got rid of a lot of dirt, but still had some caked on crap at the top and left. What kind of caked on crap? Hair. Dog hair, to be specific. And I've only hauled a dog once or twice in my time with das 'Burb. So some OLD dog hair. Whooped out an old tooth brush and scrubbed that **** off. And then sprayed and hosed again. And again... and again. Finally, after getting sliced up nicely by the evap fins, I reached this point:
You must be registered for see images attach
And with that, I said, It IS Done. I put the blower back in and reassembled the rest. Results were better airflow, less fan noise, and better smelling air. Also managed to hit around 38F with the same ambient as before. So better evap efficiency too. I'll get some better weather for testing in the near future, but I think the AC is about as good as it will get. Will be installing the condenser fan to see if I can keep the idle AC temps down.
And that's the way it was...