When your spinning the ring gear hold on to the yoke to provide resistance run it back and forth resistance both ways through the painted area....fwiw all cases are probably a little different but my 89 2wd had a .037 factory shim and it worked fine with my new 4:11 ring n pinion ....
Got a good pattern today finally ...pinion way too deep .. needed an .037 under the pinion head....I caved and bought 2 pinion bearings and made a test fit bearing for multiple tries....boy thats no joke cutting through one of those bearings lol.....ran out of time -kids +but confident I will...
I am with L31max ....I too ran the ramjet in one of my old cars in a 350 and for the expense and performance gains it wasnt worth it to me .....if your looking for more noticeable punch your going to need a better grind. I just found it to be a slight increase over the stock cam. What might...
Very informative ...thanks so much for looking this all up for me .....pictures are worth a thousand words .......simply stated pinion is in too deep ....will adjust accordingly - less shims. I should have it dialed in tomorrow finally. Ive been in and out about 10 times now lol..... An...
Night 2 lol ....have had it in and out probably 4-6 times so far ....I'm at .012 backlash currently so sneaking up on specd .008-.009... tomorrow I should have it dialed in....everyone has said your going to have to put it in and out several times which I'm finding to be true lol....
I have never done a gear change before ...so here's a few pics O tonight's work ... I was able to get the ring gear on heating it with a torch and pounding it with a rubber mallet . I got the new pinion bearing on the new pinion by heating it in a pan of oil on the stove to ~350 then I was able...
Best $35 I ever spent for this crossbolt - broken bolt extractor kit ....drilled for 2.5 minutes total time ,stopping every 30 secs to put in some lube....I put in the spiral extractor and it came out first try .....I think the key is the 2 plastic threaded guides that come in the kit and keep...
UUUgh ...absolutely horrible night in the garage tonight....got my gearset today and proceeded to do my first step and remove my cross shaft retainer bolt and it broke off in the carrier -noooooooooooooo......Apparently this is a very common occurance. So I bought an extractor kit several people...
Thanks Fancy ...yes lifes been busy so back to the toy lol....sold some parts to fund the final home stretch repairs and the rearend gear going in...then FINALLY taxes ,title , insurance and take her for her inaugural spin after all this time building it .......my goal is to be behind the wheel...
They had a few factory bandaids trying to fix this common issue....one was an oil filter that kept pressurized after shutoff lol it didn't work....the other was a prom reflash that pulled initial timing at idle reducing the knock. I can tell you from personal experience I did a carb conversion...